This is the start of a DIY rebuild project for the Tektronix PS503A dual tracking power supply.
I once build this unit a long time ago, in the late 70's, using several original parts.
An attempt to create my own dual supply many years later is described on my Blog here.
I'm showing this instrument because my plan is to use the same enclosure and the controls, but with a new PCB front panel. The PS503A does not have a display, but I'm going to use this one. After I build it, I made several changes to the way the display is used, hence the handwriting on the panel. It is actually an accurate voltmeter with an LCD. I use a switch to show either the positive or the negative voltage. The switch above with the +/-V does that. The switch labeled Tracking will tie the two supplies together such that the voltage set for the positive supply will be tracked by the negative supply. This Master-Slave method is quite common, but the Tek engineers figured out a way to select separate rail voltages and use the tracking to change the set voltages by a percentage. So you can have a rail for +15V and one for -8V and change both voltages together in a relative method, by a percentage change. That's what I will use too.
Unfortunately, the above supply, that started as a study on using the standard LM317 and LM337 regulators works OK, but not great. The main drawback is that I used a transformer that only allows +/- 100mA at 30V and the current is not enough for many of my projects.
The goals for this DIY PS503A project
The goal is to build a standalone unit that can be placed close to a prototype to supply the required rail voltages. My intention is to use this supply when I'm working with Opamps that need a positive and a negative rail.
As mentioned above, the rather special feature of the PS503A is that it not only has dual tracking, but also with two different voltages. The dual tracking in this case will supply a percentage change on both rails. More information can be found on the Tek Wiki pages here.
The SG503A goes up to +/-20V and 1A, and I'm planning to see if I can increase the voltage to +/-25V, maybe not with a 1A output, but maybe half of that above 20V. A lot will depend on the transformer, it has to fit in the enclosure. With the now selected transformer I'm limited to +/-20V, just like the original, but with a maximum current of 600mA.
The challenge with the original design of the supply is that the circuit needs Opamps that with one rail goes to the output limit plus some headroom, and also need a negative supply of several volts. This inherantly limits the maximum power supply output voltage to an output that is several Volts below the maximum Opamp +/-rail voltages. The early 741 Opamps I believe had a maximum of 36V but in reality, could not be used reliably with this limit. Most older designs I know used +/-15V rails with these Opamps.
The H-P method
More modern supplies use another method using a separate auxiliary supply for the Opamps and they regulate from the supply ground level up or down. My other Power Supply that I designed several years ago uses that method. That was actually invented by a company called Harrison that was specialising in Lab Supplies that was later purchased by H-P. The method eventually became known as the H-P method because they used it in many of their Lab Power supplies. This smart "trick" allowed engineers to build power supplies with much higher output voltages.
Applying this method to the PS503A would mean a significant demolition and reconstruction job that is beyond my plans for this supply.
Possible improvements to the PS503A
One of the items I would like to address is the over-voltage protection. The original over-voltage protection for the PS503A uses a Zener with an SCR to cut the output if it is above about 24V. That would be a catastrophic failure condition. In earlier versions, like the one I originally built, the SCR would actually short the raw supply rails with a small resistor to the common such that it would blow a fuse. That's pretty dramatic, and that method is called a crow-bar circuit. In latest version of the supply however, the SCR now cuts the drive to the output transistors, and will also discharge the output capacitor. This is a clever trick because it protects the DUT in case the power transistors fail.
There are several components that do not like a dramatic disappearance of one of the rails, it could actually damage the chip. So my plan is to see if I can couple the fault mechanism to both rails at the same time. However, after thinking some more about this, I did not pursue that and will not add that for this prototype.
The other improvement I would like to add is a tracking overvoltage protection, that would remove the output if the actual output voltage level is only a Volt or so higher than the set voltage, to protect my precious circuits much earlier and at lower voltages, which is especially critical for 5V and below rail voltages.
Building a simple prototype
To better understand the circuitry and try some of the enhancements or changes, I built the positive supply section and the voltage reference section on protoboard. I did that in several steps to test them out before adding more complexity.
Here is the complete positive supply section, working and functional with some improvements already. It does not have the over voltage protection yet. That was to be added later.
What you see here on the left is the original voltage reference section with an alternative I want to use. Next to it the dual +/-10V references (for both supplies) followed by the voltage controller and the output section. The red test lead in the middle is connected to the output terminal, which is the right side of the green 0.6 Ohm current sense resistor. To the left of that are the two output transistors. On the top right edge of the first board you can also see a device on a carrier which is the new current source.
The circuit on the protoboard on the right is the current controller. The red LED is lit, because I adjusted the output current with my Dynamic Load and dialed in the tripping point of the Current Limiter, such that the supply is now in the Constant Current mode. The original PS503A uses a little incandescent light bulb (18V 26mA) to show an indication of the output level voltage. I changed that circuit slightly and now use a yellow LED, and you see that lit on the right hand side. More about that below.
Improvements
Here is the positive supply section I prototyped and will be addressing below:
The reference supply
While I was building and testing the prototype, I noticed a few items that I wanted to address. First of all, I found that the reference supply is not as stable or resistant to sudden temperature changes, although it uses the classic form of temperature compensation. The engineers used a common trick by using a diode (CR24) in series with a Zener (VR24) to counter the voltage change due to temperature. (one has a positive coefficient, and the other has a negative effect) However, that does not work well with sudden changes, like a draft. It also takes quite some time to warm-up to a stable reference voltage. When I used my DMM on the reference voltage and briefly blew some of my breath over it, the voltage jumped before it slowly normalized again.
Granted, this will not happen this drastic when everything is warmed-up and inside an enclosure.
But, it's also not as stable as I would like to have it (see below), and worse, the +33V supply for this circuit will vary with the output load as I describe later. The 33V rail voltage can drop to 24V with a maximum load. The REF01 voltage reference will be better suited for these changes, but I may want to add a small circuit to keep the voltage constant. I need to test that later. The voltage reference chip that the engineers at the time most likely didn't have access to, or it was deemed too expensive, or deemed to be too good for the intended applications for this supply. I will most likely make both options available on the PCB, if there is enough room. There is not so I dropped that circuit.
Here is the schematic (in KiCad) for the VRef and Tracking circuit. On the left in the box the original voltage reference circuit and in the smaller box the new one.
The Vref of 9V, or in my case 10V is fed to the two Opamps, in a configuration where one is a voltage follower with the same output as the input, U1, to provide +10V for the negative supply, and U2 that changes the polarity to a -10V reference voltage for the positive supply. Yes, you're reading this correctly, it's not a mistake.
Here is the measurement that I took from the original reference voltage output.
This is after a warm-up period of about 15 minutes. It takes a very long time to settle. Note the span of 14.3mV over this 1hr period. This is not all together bad, but it also means that the output will swing with it, amplified by a factor of two. (10V reference amplified to get a 20V output)
The real test is to measure the output of the supply and include all components that could contribute.
Here is how that looks for a small snap-shot:
Not impressed with this, I used a REF01 10V reference chip to replace the original 9V reference, and this is the result measuring the output again:
The swings look much more dramatic, but the span is only 3.8mV, a 4x improvement and this was after a rather short warm-up with a reference that did not have a burn-in period yet.
Lets have a look at the various other building blocks of this instrument.
The positive supply
This schematic already shows my latest changes in it, explained next.
When you look at this schematic, you have to realize that the +/-VDC rail, that is actually shown as +/-33V in the original, and the +/-27V rail are not constant values. They are only accurate when there is no load on the output. Both voltages will go down with increasing loads and can get as low as 25V! See the section about the transformer selection below for details. The +/- 27V rails were only added as a limit to protect the 741 Opamps, and provide a maximum, but the voltages will get below that value with higher output currents.
Please note that this is still under development so can easily change. I will do my best to update the schematics as I'm progressing, but don't use them yet to build your own, give me some time to complete it first. There is now a 2.7R resistor from the cathode of Q15 to GDN, and D29 is now a 1N5401, a 2A part instead of the 1A original.
The improvements I already made
The Opamps
Instead of one of the first available Opamps, the 741 Opamps that were used in the earlier generations, I selected the TLE2141 Opamps. Mainly because I have many of them, and they can stand a 44V supply maximum, which makes it more reliable than the originals that went kaduk quite often. Even so much so that lower (+/-27V) protection rails were added to the PS503 design, and even that did not stop all the failures. This could also be contributed to the fact that the early 741's were not that reliable stemming from earlier manufacturing processes. I could have use the TL071, but that also has a rather limited maximum supply voltage specification. As a minimum, during the prototyping phase, I will be using the more rail tolerant TLE2141. It also allows me to raise the +/-6V2 voltages to +/-8V by using regulators. I have some 36V uA741CP on order so I can try the more modern versions as well (with adjusted rails). There are modern versions of the 741 available that have a 44V rail maximum, but they were not available through my preferred sources.
When you use the relatively slow 741's, you dont need frequency compensation to prevent instability or oscillations. My plan is to test them with the first prototype.
The current source/bias for the diode OR and output transistor
This step is a pre-cursor requirement for increasing the supply voltage and is better because it removes the effect of the rail swings due to the load as well.
If you look at the original schematic, I replaced the bias setting resistor (R87) to the Base of the driving transistor Q14 from a 3K resistor to a 5mA Current Sink. This will make the diode OR circuit and Base current independent of the raw supply and the variable current flow when the output voltage is changed from the minimum to the maximum. In the 20V version, that point moves from 9V to about 25V, and hence the Base current changes for Q14.
The just about standard method is to use a current source and not a resistor. In my previous design for a power supply, I used a typical circuit to create a stable current source.
Below is that circuit. It used a red LED as a rather stable voltage source to bias the PNP transistor Q2. The Emitter resistor R4 sets the current, R15 sets the LED current. The capacitor of 220uF was added as a startup glitch protection, because it delayed the bias setting until the other supplies where stable.
In that supply design, I used LED's as the diode OR because they were used on the front panel showing the CV or CC mode activity.
There are many other possibilities to create a current sink/source, but I opted to use a dedicated LTC chip (LT3092) and two resistors to precisely set the current. I already had two of them in my stash, waiting to be used. I tried it out and it works really well. By using the formula in the datasheet, I could easily select the resistor value for the 5 mA current I wanted. This is a little higher than the original current that varied between 1.7mA and 4.9mA using the resistor, but that is not very critical.
The Vref for the current limiter
Because I'm now using a different VRef circuit, I needed to change the Voltage reference (actually, the constant current) for the current limit circuit. In the original, that voltage was tapped from the VRef circuit (connection between R28 and R29), and then fed through a diode (CR78) to the base of Q80. I simply adopted the circuit from the negative supply and used that for the positive supply as well. This adds R41, Q11 and R40 in my schematic.
I noticed that by changing the unregulated supply voltage, the collector voltage of Q3 supplying current to the CL potmeter is changing only a few mV between 33V (no load) and 25V (maximum load), keeping the voltage across the CL potmeter quite constant at 750mV for the 400mA output load setting, but needs to be checked again when I will go to a higher output voltage from 20V to 30V, or the full 1A current. It may need a voltage regulator or current sink.
The Voltage output indicator
Because I don't want to use a light bulb for the Voltage indicator (old school), I'm using an LED that many users of the PS503A had to change to as well because these tiny bulbs are now hard to get. I opted for a yellow LED, and that required a value change for two resistors, R14 from 5K6 to 15K and R15 from 510R to 160K in my schematic. Both values depend on the LED current, so may need some tweaking with different LED's. I'm simply using one that I already have, but is without specifications. In my case, the LED is just off with a zero Volt output and will be bright at 20V. When the output is switched off with SW2, the current from R15 is disconnected and the LED is off to show you that there is no output voltage present. Just like the original. When the overvoltage protection kicks in, the output goes to zero V and that also turns off the LED.
Decoupling the Opamps
I also added decoupling capacitors for the Opamp rails.
Sziklai output transistor pair
The last change, for the time being, is the change of the Sziklai output transistor pair. In the original, the power transistor was in the TMXXX mainframe and is not so easy to find. I selected a combination of the BD139 and the D45H11. I had a few left from my Walt Jung voltage regulator design, and if Walt found this transistor good enough, who am I to disagree? This selection may change however when I have a real setup that will allow me to do some power stress tests later on.
If you want to know more about this Sziklai configuration and the difference or pro & cons compared with a Darlington pair, use Google.
There are two main differences that I care about. First of all the input voltage for the first transistor is 0.6V for the Sziklai and double that or 1.2V for the Darlington combo. The other difference is the thermal stability that is reportedly better with the Sziklai, and the two transistors do not need to be on the same heat sink, which was important for the original PS503A with the output transistor located in the TM5XX mainframe. The original TM5XX mainframes used the TO220 versions of the 3055 and 2955 transistors. More information about these transistors and replacements can be seen here.
Resistor value changes
Although I purchased all the required (odd) resistor values, I may change several of them to the E96 range. The reason Tek used these sometimes odd ball values, like 1K05 or 1K62 and 976 Ohm is that in those days, through-hole metal film 1% or better resistors only came in these values (not even in E192).
The BOM will show some of the alternatives.
The over voltage protection
The tracking overvoltage protection
I'm using U13 as a comparator to determine the tripping point. The output of the voltage regulator Opamp U7 is used as the reference voltage for U13. The output of U7 has almost the same voltage as the output, so varies between 0..20V. I'm also tapping the output terminal and drop that voltage by two diodes in series to create a delta between the output and the set voltage. C51 and R52 are there to provide a bias for the diodes and also a filter.
The negative supply
The Power rails
Transformer selection challenges
So what are the effects of my 24VAC 30VA transformer?
What you see on the protoboard is the bridge, a bleeder resistor on the bottom, the main capacitor, a 1 Ohm series resistor, changed from the 2R2 resistor I wanted to use, and a 2,200uF for the second capacitor, replacing the 1,000uF I wanted to use. The 2R2 got too hot, and the 1 Ohm was sufficient. The increase in the second capacitor dropped the ripple quite substantially, also making up for the reduction in the resistor. The second capacitor and the 1R resistor might not be needed for the 500mA version, but I leave it in as an option for the 1A version.
Supporting a 1A output
To the right is the new 2x25VAC with 1.6A toroid with 80VA. It is significantly larger and weighs just over 1Kg. The one on the left weighs 532gr. The heatsink will have to be mounted on the outside of the back panel, if the back panel itself is not sufficient to have enough room for the PCB. I will use the room that the 80VA will leave as the size for the PCB.
Power rail schematic
The Voltmeter
This circuit is quite simple but in order to switch the display voltmeter inputs around so we can measure the positive and the negative supplies, the power rails for the meter have to be galvanically isolated from the rest of the circuits, hence the small additional transformer. The minus input from the voltmeter is internally connected to the minus supply voltage of the meter/display, so that's why this is needed.
Next steps
Now that I have the inner workings understood (at least I think so), and verified most of the enhancements with the prototypes, I think I'm ready now with a first attempt on designing a PCB. With that comes all the sorting out of the components and footprints, so that will take some time.
I have the layout of the main board done and I'm now working on the front panel which will be a PCB as well. The layout of the controls on the rather busy front panel required a few changes to the main PCB, so I'm going back and forth to make sure it all fits the first time. I hope...
There are also some changes to the circuits and I will post the latest schematic diagrams, and screen shots of the PCB's below.
Here is the completed layout of the PCB.
I'm using TO-92 packages for the transistors so I can easily swap them out for other types if required. When that is done I could switch them out with SMD versions with a new board revision.
And here is a 3D view of the front panel - note that it will have a black solder mask:
There is a ground fill on the front and back to act as a shield and will also add some sturdiness and produce a very nice half-matt black finish. All the holes are plated through with a larger surface on the back to properly ground all potmeters and switches. The four LED's have a normal 3mm hole. I decided to not implement a LED indicating the low current setting (300mA). It's obvious from the switch setting, and the front panel is already very busy.
Another thing you may miss is the switch to activate the dual tracking feature. I found an original potmeter with the switch at a site that sells Tektronix parts, and I purchased one. Not having a switch is not that cumbersome, because you can turn the potmeter fully CW (fully up in the diagram) to the 100% setting, and that will actually be the same as using the switch.
Here are the latest schematic diagrams with the latest changes. The updated Voltmeter section is just above.
Not many changes, but I did ad a jumper to deactivate the tracking overvoltage circuit in both supplies.
At first I had room on the PCB to implement the original reference circuit, but I found out that I needed more room close to the front panel for the current potmeters. Eliminating that board space made it too cumbersome to move that circuit someplace else, now that the rest of the layout was already done, so I took it out.
Mechanical construction
Below is the old front panel that will be replaced by the new PCB. The paper copy shows the dimensions of the main PCB inside the enclosure, with now plenty of room for the potmeters and the three 4mm binding posts in the front.
The bottom side of the board with the bridges and output transistors, will be mounted flush on the metal back panel for cooling. To the right is room for the mains input receptacle and filter. The main transformer will be mounted on the top half of the enclosure, hanging down so to speak. If the cooling of the back panel alone is not sufficient, I will add a heatsink mounted to the back panel on the outside of the enclosure. At least that is the plan.
Since making this picture, I made a few more layout changes by moving the reservoir capacitors on the right side towards the edge of the board, now possible because I used a smaller transformer for the LCD display.
The two boards are now uploaded to my sponsor PCBWay, and I hope they will accept to sponsor this project as usual. They did, so the two boards are now in production. As soon as I have the boards, I will continue with the project.
The boards arrived in record time (less than a week) and look great as usual.
It took a little to find some free time, but they are now almost completely populated.
I'm still waiting for a few missing parts, but I'm almost ready to start testing.
The front panel in the background is also mostly done.
Here is the back side of the front panel with the wire harness.
Most of it is in position, although not secured in place yet. I need to verify the proper switch settings with the front panel text, and may need to rotate the switches and also the potmeters so the contacts are out of the way.
The tracking potmeter and the two current limiter potmeters are not installed yet because I needed to glue the four LED's in place and needed the room. I also need to solder the wire harness to the LED's before I can mount the three missing potmeters. I also need to wire the pos-neg switch to the display and output terminals. All these wire connections will be on the back of the panel. The main switch will be wired last.
It's a very busy looking back panel with a very tight fit and not much wiggle room left.
First Power-up
First of all, I took a look at the rails to see if they were all there. To test that, I used my Lab supply and connected both channels to the 24VAC transformer inputs. That allowed me to keep an eye on the current consumption, in case something is not right.
Well, there are several things not right, so I will have to go through the issues. I know it worked on the breadboard so that's assuring. A few things were added based on the prototype so there can be many things. I'll come back later when I have sorted it out.
What went wrong and got me stumped for a while was that I forgot that I swapped the driver transistors, so the front is close to the output transistors. I did that positioning to avoid crossing of the traces. between the two transistors. Because of this mistake, the output supply would not regulate well, and a few times I had 33V at the output. Not knowing what was going on, I disabled the over-voltage protection by removing the resistor in series with the 24V Zener diode. Unfortunately, a side effect was that blew the voltage controller Opamps that I still has as the TLE2141. I replaced them with the original LM741C Opamps. With the Opamps shorting out, I also had two casualties with the +27V rails transistors, even though I replaced the original 2N2222 with a 2N2216, and the 2N2907 with a 2N2905. During this period these transistor got too hot and I used heatsinks on them.
After rotating the driver transistors around, all was still not well but nothing was getting hot.
The other problem was caused by yet another goof from my part. I used the +/-6.4V rails to power the LT3092 current sinks. That limited the maximum output voltage. I could not easily connect them to the +/-33V rails, where they should have been connected to, so I took all the parts off the PCB and added the original 3K resistors on the back of the PCB, connecting directly to the output transistors. If/When I will go through a new layout, I will add the possibility to select either option.
I also found that I swapped around D22 and the D23 LED in the negative supply, yet another dumb mistake but easy to fix.
I then found that the two yellow voltage indicator LED's that I used, where from different models. The one I tried with the prototype (trying for both supplies) worked fine with the 160K resistor value for R15 and R22, but the LED I used for the negative supply was nowhere near as bright, so I eventually selected a 91K resistor that made it look similar, but not the same. I will need to order two new LED's to make them the same.
I had a few other connections to potmeter and switches swapped, but they also were easy to fix by changing the order of the leads in the plug headers.
Testing the operation and limits
So, with all that out of the way, I could finally start to work with the supply.
The maximum output levels of both supplies were calibrated to 22.0V to give it some extra headroom.
I used a 150R/1W resistor to quickly test the current limit circuits, by touching the output connectors. When I was happy with all the controls now working and the potmeters turning the right way, it was time to use my Dynamic Load to test the current limit minimum and maximum ranges. I always like it when I can activate the current limit in the lowest setting, but that's not the case here. At the output set for 20V, the positive CL only cut in at 10mA. This is easy to fix by lowering the value of R50 and R34 from the 680R value to a lower one. The negative supply now also cuts in at about 10mA. (the first step of my Dynamic Load)
I then performed the maximum current test. In the highest range, I measured 1.2A, a bit higher than anticipated with the original 1K05 resistors that were in the original schematic for the "hi" current mode. This can be changed by using another value for R35 and R51. I will not be able to get that high a current with the transformer I selected, so I need to recalculate the values for R51, R59, R35 and R65 for both the 300mA and 600mA current limit ranges. I'm now using 510R for the 600mA range, and another 510R that will go in parallel for the 300mA range. With these values I will actually have 630mA and 320mA, so a little head-room.
I changed the resistor values for the minimum setting (R34 and R50) , but could not get them to turn-on the CL mode with the potmeter at minimum. They still need a few mA to light-up.
Testing the limits
While still using my Lab Supply, I performed another maximum current test, but with the maximum output voltage of 20V. My Lab supply can only go up to 32V so a tad less than the transformer would provide. However, I set the outputs for a maximum current of 1.25A. With 32V DC applied at the 33VAC connectors results in a raw supply of 30V, due to the bridge, the PTC fuse and the 1R series resistor. Using my Dynamic Load, I tested the output voltage set at 20.0V with my DMM while increasing the current to see if or when the output voltage would drop. For both supplies, I could go to the maximum 610mA limit and the voltage stayed at 20.0V. At the maximum 600mA the raw voltage went down to 29.5V. This means that the raw supply input components only contribute with a 0.5V drop at the maximum current. With the maximum 600mA output, the power transistors that were mounted isolated on the 1mm thick back panel where getting warm but not hot at all. But, this was an easy test with 20V. The true test will be with lower output voltages when the voltage over the output transistors will be at maximum. I'll do that later.
Using the 30VA transformer
When I found everything functional, I swapped the Lab Supply with the 30VA transformer so I could profile the maximum voltages and currents. Now that I have the transformer in place, I also have power for the display. Because the display is actually a DMM, it is very precise.
Positive Supply:
With the transformer, the raw voltage is +32.6V at no load. The ripple at the +33V test point is 4.6mV. The +27V test point measures +26.1V, the +6.4V test point measures +6.43V.
At the 300mA output current level, the raw voltage drops down to +27.27V with a ripple of 22mV. The output is still +20.0V. The 27V TP reads 25.45V and the 6.4V TP reads 6.43V.
With the 600mA maximum current, the raw voltage drops to +23.7V, the ripple is 38mV and the output voltage is still 20.0V. There is a 3mV ripple on the +27V test pin, and the voltage is The 27V TP reads 22.78V and the 6.4V TP reads 6.43V. The 27V supply drops a little too much for comport, but otherwise, everything is good.
Negative Supply issue:
With the transformer, the raw voltage is -32.5V at no load. The ripple at the -33V test point is 4.6mV.
The -27V test point measures -26.1V, the +6.4V test point measures -6.47V.
At the 300mA output, the raw voltage drops down to -27.3V. The ripple is now 22mV. The problem is that the output voltage drops from 20.0V to 19V. It starts dropping from the 20.0V at around 220mA. At that level, there is no significant change on the -27V supply, it is still -25.55V.
With the 600mA maximum current, the raw voltage drops to -23.8V, the ripple is 34mV but the output voltage is only -15.8V, so we have a very weird issue here.
It works with the Lab Supply, but not with the transformer. Swapping the secondary leads to test a phase issue showed nothing. Even swapping the secondaries from the positive to the negative showed no difference. The DC voltages between the supplies all measure the same. What is going on here? Well, at the point where we loose regulation, I see a 50Hz mains ripple effect on the raw supply, that comes through on the negative output. The positive supply is totally devoid of this ripple all the way to 600mA. It sure looks like I have a bad reservoir capacitor in the negative supply, that did not show up when I used my DC Lab Supply! De-soldering them and measuring them with my DMM showed no issue though. I even measured the bridge, no issues. Weird!
I found the cause.
It's the startup/imbalance protection circuit around Q6. The Base of Q6 is getting the ripple and with a higher current (dropping raw voltage) it will eventually draw the diode OR down. When I disable the link to the diode OR, everything is fine. So what is the root cause? A bad Q6. In the tester it shows a diode between C-B, no E. Replacing the transistor solved the problem.
The output voltage now stays at -20.0V all the way until the maximum current of 600mA is reached.
Testing the Dual Voltage Tracking
This was easy to test. When both voltages are at the same level, you really have a dual tracking all the way up and down, the traditional way. When you set one voltage to say 15V and the other to 20V, the dual tracking will vary the voltages as a percentage. BTW, if you have the potmeter without the switch, you can still use it as in "without dual tracking" or disabled, just always remember to rotate it fully clock wise.
We have a working unit!
Testing the over-voltage circuits
driver transistors, but wanted to verify them now that we have a fully working system, using the transformer.
Turning the supply on or off
Testing the over-voltage tracking circuits
I used the same technique using my Lab Supply to raise the output voltage a bit above the set voltage to trigger the over-voltage tracking circuit.
When I set the output at +10.00V, applying +11V triggered the protection. I had to make one small modification to the circuit though. Because the U13 Opamp does not go all the way to 0V when not triggered, but has approx. 115mV, it already triggered the SCR. Instead of the jumper, I installed a 47K resistor to lower the voltage and that worked well.
For the negative supply, using -10V at the output, triggered at -11V, but because this circuit is quite different from that of the positive supply, I needed to use a 4K7 resistor instead of the jumper to make it work.
Testing the max and min voltages.
Setting the supply to +20.00V, +21V triggered the protection. Setting the output to +1.80V, and applying +1.9V triggered it also. Seems to be working well. I need to try this in real applications but I will also install a switch on the back panel to activate or de-activate this feature.
In the next revision, I'll add a third diode to create a bit larger delta for the trigger voltage.
Maximum current stress test
To see the thermal development during the maximum current, I set the output to 5V and used my Dynamic Load to pull 600mA. Unfortunately, the output transistor gets too hot. After about 10 minutes, it was approaching 150C when I stopped. In an earlier test, I decided to mount an extra heatsink on the back of the metal back panel, but it's not enough. Especially when both channels are used. The rather large and seemingly oversized bridge rectifiers are getting pretty warm too. They will need the extra cooling assistance by mounting them on the back panel, as I already intended. Unfortunately, this reduces the room on the small back panel considerably.
I need to think about possible solutions so I don't have to use forced cooling by a fan. I really like to avoid that but it may be my final resort.
I'm first going to "bolt" the heat sink that was used in one of my earlier power supplies to the back of the back panel, in the hope it will be sufficient.
Next revision PCB
With the changes I had to make, plus the fact that I now have decided the use the 30VA transformer, several components can be made smaller due to the lower current. I will also change a number of the TH parts to SMD now that I have a better handle on the power consumption.
Keep coming back regularly, I will be adding or changing information as I go about designing the rest of the project.
More later....